Sunday 30 June 2013

Test run 29.6.13 and 30.6.13

Fitted a solar charge controller and re fitted the small solar panel on the roof as the batteries have been holding charge well. The solar panel must have been causing problems to the charge circuit so will not be plugged in during cruising. The boat started well and it is a lot quieter at high revs since the exhaust was repaired. Took it to Mercia for 10 mins to blow off the cobwebs. We are taking it out tomorrow for a short cruise. Took the boat out this afternoon and got the click on trying to start the engine again, but it turned ok after a few turns - will try fitting the new battery, but, starting to think that the starter motor might be on the way out.

Monday 24 June 2013

Top of steps

Decided to put a new ply panel on top of the steps - existing panel is very thin ply and is delaminating as well as the hooks becoming less secure - the screw threads have got loose, the chipboard behind has also bulged out. Using long wood screws has pulled the wood sections together and made the surface solid to hold the steps and hooks in place.

Saturday 22 June 2013

Exhaust repair

 I cut off the insulating bandage of the lower section of the exhaust and noted that there was no flexible section in the exhaust - this means that the exhaust is being stressed by any engine vibration. I noted that the original exhaust that looks about 4mm thick from the manifold had been sleeved with cheap bendable pipe and had been riveted to the manfold pipe. The cheap pipe had sheared at the end of the overlap section and was only held in place by a thin thread. The cheap corrugated pipe was 45mm. I went to midland chandlers and would have had to replace the whole system with screw fitting pipe and manifold, including a flexible section. In the end I decided to go for a cheaper temporary option of a repair sleeve available from a motor factors. The sleeve has substantial pair of bolts and I put some repair putty in the joint - clean break to assist the seal. After tightening I put more putty around the edges. On starting the boat I noted it was a lot quieter and I will be less embarased to cruise now as it was very noisy at high revs. I then replaced the bandage on the exhaust after checking for leaks. A good day and I hope the repair last for the rest if the year. The battery isolation is working as the boat started first pull.


I also bought a battery operated pump to empty the bilge fully as the bilge pump leaves about 1.5 inches of water in.

Saturday 15 June 2013

A few more jobs


Boat started ok today - isolating the starter battery is the way forward - the leisure must be on the way out - I will isolate the starter when not cruising. 

I used one of those unscrew isolators to break contact on my last boat. 

I also noted that the exhaust was black near the engine manifold - on starting the engine a large amount of black smoke blew out nr the manifold. On the plus side it is a short length so won't be too difficult a job. Strange that both of our cars have had new exhausts recently.

Also bought a new starter battery as back up.

I also fitted a shelf under the sink - this has doubled my storage space and made it much tidier. 

The only down side of the day was when I kicked over my dab radio and broke it!


Monday 10 June 2013

Willington raft race 8/6/13

Annual raft race between Newton solney and willington on the Trent. The village gets very busy with the 3 village pubs putting on outside bars and bands on. The Trent was still choppy - must be bad when the weather is not so good - after completing the course the rowers get pelted with eggs from the bridge. The race is a time trial but you still get competitive overtaking and collisions